Poly Plug GTL Heirs #3
Well Information
Vermillion Parish
8 1/2″-12210′
WBM
17.4
210 F
3 1/2 hrs
Challenge
Total losses–2500+ bbls of mud had been lost to the formation. The offset
well required 4 cement plugs to control losses. Two Poly Plug pills were
pumped with 40% returns noted after the first pill and 100% returns after
the second pill. Drilling commenced to T.D.